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HomeMy WebLinkAboutL202501 NOPV Response LOWER YAIIFY_® - E N E R G Y 136 N.Washington •P.O.Box 188 •Afton,WV 83110•307-885-3175•fax.307-885-5787 Jeff Brooks October 23, 2025 State Of Idaho —Public Utilities Commission 11331 W. Chinden Blvd. Ste 201 A Boise Id. 83714 Subject: Crow Creek Pipeline Construction Inspection—Lower Valley Energy Report # L202501 & L202502 Dear Mr. Brooks: Here are the responses to the items of concern discovered during inspection of Lower Valley Energy's Crow Creek Pipeline project, conducted Aug 25-26 & September 15 -16. Items of Concern: 1. Both company and contractor personnel had been actively involved in Butt fusion operations and pipeline installation. No documented procedures specific to the construction of transmission lines were made available. 2. During pipeline staging activities, multiple lengths of fused pipe were positioned above the Spider Plow equipment. The pipe traversed the terrain; where it encountered obstructions including rocks and debris. One segment made direct contact with the Spider plow blade during its decent. 3. Individuals assigned to inspect or evaluate joints in plastic piping systems must possess documented qualifications — obtained through formal training or demonstrable experience — specific to the joining procedure being performed. The individual who conducted destructive testing on butt fusion joints prior to August 28 did not possess the requisite qualifications for that procedure. The induvial was limited exclusively to socket fusion and did not extend to butt fusions. 4. Certain individuals who had performed Butt fusions were not qualified in accordance with the Record of Pipe Joining Qualification Test form. The premature certification of destructive testing activities without access to the necessary equipment undermines the credibility and regulatory validity of the qualification records in question. 5. A material discrepancy was identified within the record of pipe joining qualification test documentation. The records indicate that destructive testing was conducted in June 2025, however it was confirmed that the testing equipment was not available until August 2025. 6. LVE's Welding-Fusing-Manual referenced WL Plastics procedures but that has not been included among the procedures referenced within the manual. 7. During fusion operations, pyrometers were used to verify the surface temperatures of heating tools. These instruments lacked valid and current calibration documentation. 8. Staff found both heating plates in use during fusion operations had substantial accumulation of plastic residue. Also, on Report#L202502 9. Section H in heat fusion procedures revealed that the manual did not include mandatory inspection of melt surfaces for defects such as concave profiles, bubbling, or pocket- marking prior to the joining process. Joining procedures must incorporate quality control measures that adequately address pre join surface conditions. Response: LVE recognizes each item of concern. Each concern will be addressed below. 1. Procedures were updated when the Teton Village line was installed which included 4710 Section H. (Welding fusing procedures heat fusing Procedures W/F &M -H.) The incorporation of 4710 updated in 2017 recognized the construction of transmission lines because LVE used 4710 only as transmission. All distribution lines are yellow 2406 pipe. Transmission was implied in our procedure when 4710 is used, however, to clarify that I have updated the Welding and Fusing procedures and Construction Manual procedures to clarify that 4710 is Transmission, and 2406 is Distribution. This was referenced in our Construction manual CM-C 1 which has also been updated. 2. During the start of construction, we noticed an area of concern of pipe damage during unloading, stringing and installing which we corrected. Due to this we trained and had an inspector walk the line measuring all damage to the pipe. The inspector marked all areas of concern and then Todd as a qualified inspector verified all areas of concern and cut out anything that warranted removal. We also had our Inspector, fusers and spider plow operators checking for any gouges or issues with the pipe prior to installation. We did cut out over 15 areas of concern. We also contacted Pipeline Plastics who gave us guidance on pipe damage evaluation. "In accordance with industry practice PLP recommends the maximum allowable damage to a pipe is no more than 10%of the thickness of the wall. Due to cuts scraps gouges or abrasions. This 10% is considered the industry's best practice as recommended after thorough research and investigation. This number represents a conservative recommendation based on that research." We replaced all abrasions scraps and gouges that were 5% or more leading to a higher standard than the best practice considered by Pipeline Plastics. POWERFUL1 r a•. 3. The absence of any socket fusion on this project would indicate that the paperwork was filled out incorrectly. The paperwork should have indicated Butt fusion instead of Socket fusion. That paperwork has been filled out correctly. The individual that the paperwork was wrong with does have 25 years of experience and was quilifed but the error in paperwork was wrong and corrected. 4. We did use Accel fusion for fusing who had all qualification needed to perform the task. Westwood's crews had training from ISCO prior to any fusing. The individual who had performed Butt fusion was qualified but incorrect paperwork was filled out. 5. LVE did not have the stress test machine and had filled out the paperwork which was wrong and will not happen again. Since we got the machine, we did catch up on all testing and have tested as needed, on time, and filled out the paperwork correctly. Proper record keeping is essential to showing that things are done correctly. 6. LVE's Fusing Procedure Manual and Construction Manual has been updated to reference WL Plastics joining and field procedures and McElroy's app for fusing. It is noted at the end of section H in the Welding and Fusing Manual Plexco's practices which include Performance Pipe for fusing. 7. During fusing, pyrometers were being used but there were no calibration records for those pyrometers. To correct that LVE ordered new pyrometer with the proper calibration paperwork and used those going forward. 8. Our procedures require heating plates to be clean before fusing. This area of concern was addressed, and all machines put on new plates which were cleaned daily and inspected by LVE's inspector. All fuses from the Acccel fusion machines were data logged and had to pass the test for proper documentation of a good fuse. 9. The manual did include mandatory inspection of melt surfaces for defects such as concave, profiles, bubbling or pock marking referenced in section H under Driscoplex which is also part of Performance Pipe. We did add clarity the end of Section H where it references Performance Pipe with Driscoplex reference which does address surface defects. LVE has never had a fusion failure with over 250 miles of fused pipe. However, due to some of these concerns LVE �vjll leak survey the Crow Creek Transmission line 2 times in 2026 at our MAOP of 125 psi to insure the safe operation of our new natural gas pipeline. Thanks for working with Lower Valley to help us be compliant with the federal code and more effective in our responsibilities of working safely and according to best practices. LVE is confident that we will continue to create a safe working environment and to comply with all regulations at our facilities. Give me a call if you have questions at 307-885-6151 or my cell at 307-248-2885. Hope you have a nice day. Sincerely, C_ IZ,, Craig Coles Director—Gas Operations cc: Jim Webb