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HomeMy WebLinkAboutIntermountain Gas 240122 Meridian Construction IPUC Construction Inspection Inspector(s): Galli, Brooks Date(s): 01/22/2024 Company/Owner: Unit/OPID: 08160 Intermountain Gas Company(IGC) Address: 4610 S Hennessy Ave City/District: Meridian Contractor/Job #: Foreman: Employees: See Job List 117904-425 Darcy Ugalde Job Description: Install '/" Service Line System Type: ® Distribution ❑ Transmission Operator Supervisor: Jason One-Call Ticket: 030720 On-Site: N Total Inspection Days: 2 Tasks: Rating , Critical Procedure# Comments 1. Materials—Handling, Storage, SAT OPS 11 Labeling 2. Trenching/Boring—Depth, Clearance SAT OPS 308 OPS 322 3. Bedding/Backfill SAT OPS 308 Sand used SF 418 4. Pipe Installation (Tracer Wire) SAT OPS 308 OPS 322 5. Valve Installation N/A OPS 703 6. Coating Condition N/A OPS 401 OPS 403 7. Manuals—Field Procedures, O & M SAT 8. Testing—Pressure, Duration, Type SAT OPS 505 98 psi for 15 minutes 9. OQ Qualifications SAT OPS 800 10. Casing Seal/Installation N/A OPS 325 11. Service Line Installation SAT OPS 302 12. Tie-In/Hot Tapping N/A OPS 600 13. Meter Location/Regulator Testing SAT OPS 302 14. Equipment Calibration Verification SAT OPS 501 See pictures 15. EFV Installation SAT OPS 301 EFV 1200 16. MAOP N/A OPS 602 OPS 606 OPS 900 OPS 1000 17. Pure N/A OPS 603 18. Safety Equipment SAT SF 418 SF 422 19. Abandonment N/A OPS 607 20. Line Locating SAT �� OPS 611 I P U C Form 4 Rev. 12/21/2023 IPUC Construction Inspection 21. Plastic Pipe SAT OPS 307 - Joiner(s) Qualified OPS 309 - Fusion Tools OPS 324 - Heat Plate OPS 325 - Joining Procedure OPS 800 22. Steel Pipe N/A OPS 200 - Welder(s) Qualified OPS 201 Pipe/Coating—Inspected/Repaired OPS 202 - Cathodic Protection OPS 306 -Non-Destructive Testing OPS 401 - Welding Procedures OPS 407 - Removal of asbestos wrap OPS 402 - Exothermic Welding OPS 403 4800 Additional Comments: IPUC inspector Galli and Brooks observed Das-Co, a contractor for IGC install a 3/' service line in Meridian, ID. Address: 4610 S Hennessy Ave, Meridian ID Observations Include: correct trench depth, safety equipment, verification of OQ records, verification of equipment calibrations, tracer wire, EFV 1200 installation, butt fusion, successful pressure test at 98 psi for 15 minutes,bedding with sand and backfill. Das-Co employee recognized the test fitting on the riser had an abrasion which caused a small leak during the pressure test. The test fitting was replaced and a successful pressure test was completed. All observed procedures were followed in accordance with IGC Operations and Maintenance Manual. Corrective Action Required: Yes No X Follow-up Required: By Date: T Yes No X Inspector(Lead): ' ' Date: 1/22/2024 Galli Reviewer: -•• - Brooks Date: p- _ ,Dq IPUC Form 4 Rev. 12/21/2023